墨西哥灣深水水平井鉆井平臺(tái)起火沉沒事故

[加入收藏][字號(hào): ] [時(shí)間:2010-05-27  來源:博研論壇  關(guān)注度:0]
摘要:   You may have heard the news in the last two days about the Deepwater Horizon drilling rig which caught fire, bur...


  You may have heard the news in the last two days about the Deepwater Horizon drilling rig which caught fire, burned for two days, thensank in 5,000 ft of water in the Gulf of Mexico.  There are still 11 men missing, and they are not expected to be found.  
The rig belongs to Transocean, the world’s biggest offshore drilling contractor.  The rig was originally contracted through the year 2013 to BP and was working on BP’s Macondo exploration well when the fire broke out.  The rig costs about $500,000 per day to contract.  The full drilling spread, with helicopters and support vessels and other services, will cost closer to $1,000,000 per day to operate in the course ofdrilling for oil and gas. The rig cost about $350,000,000 to build in 2001 and would cost at least double that to replace today.


Nautilus, being transported on a Heavy-Lift vessel


  The rig represents the cutting edge of drilling technology.  It is a floating rig, capable of working in up to 10,000 ft water depth.  The rig isnot moored; It does not use anchors because it would be too costly and too heavy to suspend this mooring load from the floatingstructure.  Rather, a triply-redundant computer system uses satellite positioning to control powerful thrusters that keep the rig on station within a few feet of its intended location, at all times. This is called Dynamic Positioning.
The rig had apparently just finished cementing steel casing in place at depths exceeding 18,000 ft.  The next operation was to suspend the well so that the rig could move to its next drilling location, the idea being that a rig would return to this well later in order to complete the work necessary to bring the well into production.
It is thought that somehow formation fluids – oil /gas – got into the wellbore and were undetected until it was too late to take action.  With a floating drilling rig setup, because it moves with the waves, currents, and winds, all of the main pressure control equipment sits on the seabed – the uppermost unmoving point in the well. This pressure control equipment – the Blowout Preventers, or ‘BOP’s” as they’re called, are controlled with redundant systems from the rig.  In the event of a serious emergency, there are multiple Panic Buttons to hit, and even fail-safe Deadman systems that should be automatically engaged when something of this proportion breaks out.  None of them were aparently activated, suggesting that the blowout was especially swift to escalate at the surface.  The flames were visible up to about 35 miles away.  Not the glow – the flames.  They were 200 – 300 ft high.
 

上一頁12345下一頁


          您的分享是我們前進(jìn)最大的動(dòng)力,謝謝!
關(guān)于我們 | 會(huì)員服務(wù) | 電子樣本 | 郵件營銷 | 網(wǎng)站地圖 | 誠聘英才 | 意見反饋
Copyright @ 2012 m.1314163.com Inc All Rights Reserved 全球石油化工網(wǎng) 版權(quán)所有
京ICP證120803號(hào) 京ICP備05086866號(hào)-8 京公網(wǎng)安備110105018350
主站蜘蛛池模板: 色窝窝亚洲AV网在线观看| 最近中文字幕高清2019中文字幕 | 好爽好多水好得真紧| 欧美黑人疯狂性受xxxxx喷水 | 5x社区精品视频在线播放18| 亚洲国产成人99精品激情在线| 国内精品久久久久久无码不卡| 欧美成人在线影院| 香瓜七兄弟第二季| 99久re热视频这里只有精品6| 午夜成人免费视频| 日本h片无遮挡在线观看| 男人下面进女人下面视频免费| 日本在线高清视频| 2021国产精品自产拍在线观看| 不卡av电影在线| 亚洲丁香婷婷综合久久| 亚洲国产91在线| 亚洲AV乱码中文一区二区三区| 国产日产久久高清欧美一区| 手机看片久久国产免费| 日本高清乱理伦片中文字幕啊| 老阿姨哔哩哔哩b站肉片茄子芒果 老阿姨哔哩哔哩b站肉片茄子芒果 | 欧美日韩一级二级三级| 天天在线天天综合网色| 一区二区三区四区国产| 久9久9精品视频在线观看| 亚洲国产中文在线视频| 亚洲小说图片视频| 人人妻人人澡人人爽欧美一区 | 欧美精品一区二区三区久久| 男女裸体影院高潮| 真实的国产乱xxxx| 精品福利三区3d卡通动漫| 能在线观看的一区二区三区| 4ayy私人影院| 2019国产精品青青草原| 草草影院www色欧美极品| 老司机精品免费视频| 亚洲五月综合缴情婷婷| Channel|